Study on Instable Combustion of Solid Rocket Motor with Finocyl Grain Study on Instable Combustion of Solid Rocket Motor with Finocyl Grain

Study on Instable Combustion of Solid Rocket Motor with Finocyl Grain

  • 期刊名字:兵工学报(英文版)
  • 文件大小:
  • 论文作者:HU Da-ning,HE Guo-qiang,LIU Pe
  • 作者单位:Northwestern Polytechnical University,The 210th Institute of Second Academy
  • 更新时间:2023-01-17
  • 下载次数:
论文简介

The instable combustion or oscillation combustion which occurs in three high capacity solid rocket motors using high energy composite propellant with finocyl grain is studied. The reasons of the acoustic combustion instability are also discussed. Three engineering methods that can eliminate combustion instability are proposed and discussed. The study shows that the combustion instability mainly depends on the propellant grain shape and nozzle structure. Some measures to reduce the acoustic energy and mass generation rate of combustion gas can be adopted. The test results indicate that the modified rocket motors can significantly eliminate the instable combustion and improve the motor internal ballistic perform-ance.

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